Artículo
A major leak in a crude oil tank: Predictable and unexpected root causes
Fecha de publicación:
06/2019
Editorial:
Pergamon-Elsevier Science Ltd
Revista:
Engineering Failure Analysis
ISSN:
1350-6307
Idioma:
Inglés
Tipo de recurso:
Artículo publicado
Clasificación temática:
Resumen
A 2000 m 3 washer tank at a crude oil treatment plant suffered a structural collapse, involving total loss of integrity. A fast fracture initiated in a sector of the shell with a severe thickness reduction due to combined internal and external corrosion. The fracture bent and propagated horizontally, at the shell-roof intersection and at the joint between second and third courses, causing the almost instant opening of a large window. Due to the large initial leakage flow, the containment enclosure wall could not hold the spilled mixture of water and crude oil. The fast leaking wave damaged the breakwaters at the top of the wall, overpassed the enclosure and pushed out a sliding gate, thus causing total liquid leakage. Fracture and computational fluid dynamics models were developed to understand the origins of the failure, as well as to reconstruct the sequence of events. Deficiencies in tank construction, maintenance adequacy, and corrosion prevention were found to be the main root causes of the failure.
Archivos asociados
Licencia
Identificadores
Colecciones
Articulos(CCT - LA PLATA)
Articulos de CTRO.CIENTIFICO TECNOL.CONICET - LA PLATA
Articulos de CTRO.CIENTIFICO TECNOL.CONICET - LA PLATA
Articulos(CIMEC)
Articulos de CENTRO DE INVESTIGACION DE METODOS COMPUTACIONALES
Articulos de CENTRO DE INVESTIGACION DE METODOS COMPUTACIONALES
Citación
Cirimello, Pablo Gabriel; Otegui, Luis Jose; Ramajo, Damian Enrique; Carfi, Guillermo Rodolfo; A major leak in a crude oil tank: Predictable and unexpected root causes; Pergamon-Elsevier Science Ltd; Engineering Failure Analysis; 100; 6-2019; 456-469
Compartir
Altmétricas